commiserations dude i know how it feels
![Wtf? :wtf:](./images/smilies/icon_wtf.gif)
Yeah it was going so well. Was having fun with a 1000 kawa on the way down.. Massive double legger through first 3 gears too..redzone wrote:fuck. similar problem i had with my gemini motor before jambo. on mine the cam dowel wiggled forward out of the cam drive. fix for mine is a longer dowel and a washer to hold it in place so it cant move...
commiserations dude i know how it feels
I want this thing to hold 2nd gear limiter launches...
was OLDie's head from a 2.4L ?New head has a cam. Ralliart copy, 35/70 70/35
Picked up my head/studs/adj cam gear off Rad last night.
Used proper headstuds this time, not twincam ones.
Doug @ NPC is re-drilling my flywheel to fit a skyline size clutch. 5 puck brass button ceramic... $825 later haha
so 2.4L made same power at approximately half the boost, same turbo. Wow!296.5 rwhp on 11psi, creeping to just under 13psi
Bolded is my replies, easier that way lol.quest wrote:you really did go all out!! Good to see serious SOHC efforts
Had to read over this thread again, as it has some really good technical info buried throughout. A few questions..
is that a custom CAS adapted to a staz dizzy or modified oe electronics from another mitsu application ?
The CAS is a mitus item, we had to get a new one as it died on us during tuning. I can get pics close up and part numbers if you wish sometime this weekend.I want this thing to hold 2nd gear limiter launches...
...with a staz gbox ? must have wrong diff gears then. What ratio is it?
On the back of the diff it says "G4 3.308" and some jap writing. Scorp Diff. Now CIG. Was in very good condition when we pulled it apart last weekwas OLDie's head from a 2.4L ?New head has a cam. Ralliart copy, 35/70 70/35
Anyone recall the chamber cc size ?
Is "Surecam" the grinder ? ...not heard you guys mention them before.
Yep was a 2.4L. Surecam made the custom cam i bought off him. Didn't use the ralliart copy. No idea on chamber cc size sorry.
Picked up my head/studs/adj cam gear off Rad last night.Used proper headstuds this time, not twincam ones.
Any part number for the 'proper' sohc head studs ?
You'll have to ask Rad, they were just wrapped in a dishcloth when i got them. Had to grind out the tappet cover a bit so it'd fit. But they definately are longer.
Doug @ NPC is re-drilling my flywheel to fit a skyline size clutch. 5 puck brass button ceramic... $825 later haha
Probably could have gone from the 225mm up to the 240mm used on our widebodys, and used an inexpensive proven clutch from the states. If they stand up to the torquier 2.6L in the heavier starquest pig, they should suit you fine.
Dunno about those 2nd gear launches tho :)
Probably could have, but i like this clutch so far. Very very harsh, especially with the locker but i was getting used to it after 1500km.
so 2.4L made same power at approximately half the boost, same turbo. Wow!296.5 rwhp on 11psi, creeping to just under 13psi
Pity your dynos hardly ever show the ft-lbs torque plotted vs the rpm scale, so one can really tell what a motor is doing
Leave it with me, i'll try get that for you :)
really cool setup!
On the back of the diff it says "G4 3.308"
I think I recalled reading where u checked the block clearance with playdoh. What about the head, for piston-valve interference ?Now i need to figure out what went wrong
Still unsure what has happened..redzone wrote:didnt u say a dowel came out? i think the dowel thing is a symptom caused by heavy valve springs, i've seen it on a few different motors now, never with stock springs. the gem for example runs 180psi seating pressure..
When it killed the old motor, we tried swapping injectors and the wiring between 2&3 at different times to diagnose the problem. Still stuffed up on the one pot. (This was the motor that had a jet valve head, jet valve leaked oil into mixture, leaned it out, pop hole in valve.)RiceThief wrote:Im thinking that your 3rd injector has a problem or the wiring to it is loose somewhere.
Let me confirm this, with your new setup you swapped injectors 2 and 3 with each other as well as the associated wiring, i assume your autronic is fueling in batch fire mode? Are you still running the pcv into the inlet?Anchor wrote:When it killed the old motor, we tried swapping injectors and the wiring between 2&3 at different times to diagnose the problem. Still stuffed up on the one pot. (This was the motor that had a jet valve head, jet valve leaked oil into mixture, leaned it out, pop hole in valve.)
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