Dead JA
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- almost postwhore
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Phil,,, did the car get spark when the ignitor was stuffed?
Also would u know what replacement part it is, like brand, part number?
Also would u know what replacement part it is, like brand, part number?
-JA Starion with JD bits , Forged engine, Heaps of mods (parked up)
-BFII XR6 Turbo Ute , Here comes 400hp for 2k :p
-77 Mazda 323 drag car. 13bt rotary project.
Yes i have too many toys.
SOHC POWER
-BFII XR6 Turbo Ute , Here comes 400hp for 2k :p
-77 Mazda 323 drag car. 13bt rotary project.
Yes i have too many toys.
SOHC POWER
- Starion_Turbo
- Enthusiast king
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if its given way between 2 cylinders then you won't see either water or oil leaks as there are no galleries betwen the cylinders.
Powerplant: Chipped stock ECU, 2044cc, 8.5:1, head intake enlarged and polished, exhaust manifold enlarged,
Balance-shafts eliminated, Intercooled, TC06 @ 10psi, 2.5" high flow exhaust system and dump pipe.
Balance-shafts eliminated, Intercooled, TC06 @ 10psi, 2.5" high flow exhaust system and dump pipe.
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- almost postwhore
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- Joined: Tue Jan 25, 2005 10:46 pm
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Cars still dead.
Heaps of compression
Plenty of spark
Its getting fuel
Just wont run.
has new coil and ignitor
crank/cam/dizzy timing is spot on
Heaps of compression
Plenty of spark
Its getting fuel
Just wont run.
has new coil and ignitor
crank/cam/dizzy timing is spot on
-JA Starion with JD bits , Forged engine, Heaps of mods (parked up)
-BFII XR6 Turbo Ute , Here comes 400hp for 2k :p
-77 Mazda 323 drag car. 13bt rotary project.
Yes i have too many toys.
SOHC POWER
-BFII XR6 Turbo Ute , Here comes 400hp for 2k :p
-77 Mazda 323 drag car. 13bt rotary project.
Yes i have too many toys.
SOHC POWER
Try changing the spark plugs.. My sparkplugs looked OK and was igniting, but the car would start, got new spark plugs and it started right away :) just a tip..JD_Stazza_Brendan wrote:Cars still dead.
Heaps of compression
Plenty of spark
Its getting fuel
Just wont run.
has new coil and ignitor
crank/cam/dizzy timing is spot on
vroooom pttshhh!! :D
3 things for a car to run fuel compression and spark.By the sounds of it you have really gone over the car with a fine tooth comb .I think maybe a few more tests to just to double check these 3 things might show up a weekness somewhere.If nothing shows up can you log anything with your ecu? Good luck and let us all know what it ends up being.
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- Austarion Occupant
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What a bitch of a problem. Hope you sort it.
Don't know whether this is a clue, but you wrote:
You didn't recently change this? You don't have any fuel leaking? Something to check out...
Don't know whether this is a clue, but you wrote:
I'm a bit concerned you've got a clear fuel filter, these cars being EFI, run high pressure in the fuel lines, meaning you should have an EFI type filter that can handle the high pressure. If you've been running with a standard filter, I have no idea how you managed to keep the lines connected to it, particularly on the inbound side.JD_Stazza_Brendan wrote:The fuel filter is a clear one that sits in the engine bay, Looks like its full of fuel. Ill swap it over anyway.
You didn't recently change this? You don't have any fuel leaking? Something to check out...
Reduce fuel costs by 15-20% & cut emissions by 1/3rd...
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Increase engine performance & prolong engine life...
How?
Click the website button below & watch the 3 minute video.
the problem my be that it's not receiving the right signal from the dizzy,
so all the events are out of wack, try a different dizzy see if that works.
I've worked on this car befor and the wiring's a mess if it isn't the dizzy it
it could be anything.
cheers shaun.
so all the events are out of wack, try a different dizzy see if that works.
I've worked on this car befor and the wiring's a mess if it isn't the dizzy it
it could be anything.
cheers shaun.
1982 JA Starion. LSD, wolf 3D, JD tc05 Turbo,(STD)cam, Double Valve Springs, 91 Galant MPI,42lbs/hr injectors, (STD)Galant Throttlebody, 4x EL Ford Coils, 400x500x95 PWR FMIC, 2.5" exhaust,Wolf Boost Controller, Balance Shafts Eliminated, Wolf Wideband o2.
?rwkw @ 14psi, 13.96 sec @ 95.94mph 1/4mile.
?rwkw @ 14psi, 13.96 sec @ 95.94mph 1/4mile.
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- racking my brains
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yes get a timing light and see where it is firing when ur cranking it.
and that igniter looks like an early magna one. they usually are tough as nails.. maybe check your ecu isnt charging the igniter too hard??
and that igniter looks like an early magna one. they usually are tough as nails.. maybe check your ecu isnt charging the igniter too hard??
Fibreglass airdams $370, fibreglass front bumpers $260, reco drag links $165, alloy radiators $925 (unpolished), h/l switch rebuilds $125, all plus freight.
Coxs Automotive (07)54433507 3/5 Service st Maroochydore Q
www.facebook.com/coxsautomotive
www.coxsautomotive.com.au
Coxs Automotive (07)54433507 3/5 Service st Maroochydore Q
www.facebook.com/coxsautomotive
www.coxsautomotive.com.au
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- almost postwhore
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- Joined: Tue Jan 25, 2005 10:46 pm
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It cant be spark as it throws a powerful blast (ask the guy from work this he will tell ya lol)
Its got great compression
Its got fuel (although i dont know how much)
I would change the dizzy with a spare ive got but the wires that go to the dizzy disappear into the shithouse wiring loom. It does seem that it might not be sparking at the right time. Gotta steal my timing light back from my dad.
All the spark side of the ignition seem to be perfect.
Its had new plugs put in. (even though the ones in the car were only 2 months old anyway)
pulled the lid off the LINK computer to see if there was any circuit board damage and it looks perfect, no broken solders, all capacitors in good nick.
Checked MAP sensor line for blockage
Cars booked into a workshop to be looked at and most likely getting the Link rewired. ive got about a week before i drop it off.
Im getting desperate, im driving a busted 2L sigma to work and it sucks
Its got great compression
Its got fuel (although i dont know how much)
I would change the dizzy with a spare ive got but the wires that go to the dizzy disappear into the shithouse wiring loom. It does seem that it might not be sparking at the right time. Gotta steal my timing light back from my dad.
All the spark side of the ignition seem to be perfect.
Its had new plugs put in. (even though the ones in the car were only 2 months old anyway)
pulled the lid off the LINK computer to see if there was any circuit board damage and it looks perfect, no broken solders, all capacitors in good nick.
Checked MAP sensor line for blockage
Cars booked into a workshop to be looked at and most likely getting the Link rewired. ive got about a week before i drop it off.
Im getting desperate, im driving a busted 2L sigma to work and it sucks
-JA Starion with JD bits , Forged engine, Heaps of mods (parked up)
-BFII XR6 Turbo Ute , Here comes 400hp for 2k :p
-77 Mazda 323 drag car. 13bt rotary project.
Yes i have too many toys.
SOHC POWER
-BFII XR6 Turbo Ute , Here comes 400hp for 2k :p
-77 Mazda 323 drag car. 13bt rotary project.
Yes i have too many toys.
SOHC POWER
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- Woodwide
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- almost postwhore
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- I've been here before
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you sure u just didnt run out of fuel?Its got fuel (although i dont know how much)
if u are sure u have plenty of fuel, im thinking its a fuel flow problem... had a similar prob on an old car a while back and it was a fuel hose that was blocked.
JB Starion - 2 tone Maroon/Silver, L300 MPI, KKR 430, Simmons, RX7 550cc, bosch 044 fuel pump..
194.7HP atw!!!
194.7HP atw!!!
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